The outter bearing, the one on the yoke side, should slide over the pinion. It is not a press fit, and it should not take but a little bit to move it down the shaft. It needs to be able to move durring the assembly process to get the preload correct.
-Ron
This is the source of much argument on the Internet as well as service manuals. There are tonnes of threads about this question and there are always a few people who say "the outer bearing should just slide right on", and then 50 other guys insist that it must be a press fit. Some guys argue that if it doesn't just slide on, give it a light sanding on the inner race surface until it DOES just slide on, and then more guys start yelling about why you can't do this.
I don't believe anyone on either side now, but I figure no matter what, pressing it on with the pinion nut isn't the right answer and I can't think of any other way to get it on there, so I'll be sanding down the next one.
Got a dead blow? You can drive the yoke down with the deadblow. How much preload did you put on the carrier? Did you have to fight it to get it in?
I thought about this, but if the force required to press that bearing on is greater than what the pinion nut can deal with, I'm not sure I want to be putting MORE impact force directly into the ring gear. Heard other guys say they destroyed their ring/pinion gears by doing this.
When I'm installing the bearing that's next to the yoke, I always use the old nut from the old gear set, because it is usually easier to install. Or if the nut is damaged, I have gone to hardware store and picked up a normal nut that will spin right onto the pinion. Just like you, I stripped out pinion threads before, so lesson learned.
I started with the nut I'd used for setup so it had no resistance on the threads. It started stripping so I tried a new nut, it went on much easier than it came off
That said, I took a break and a cooldown as I was raging all over the garage and yelling at squirrels about this for an hour.
Came back to it, pulled off the old nut, ground off the end of the pinion and re-built EVERY SINGLE THREAD that had enough on it to bother rebuilding. Then put the pinion into the housing again, held up the axle with stands and pointed the pinion down to the ground, installed the outer shims, bearing, baffle, and yolk, then rested the whole thing on my welding gloves and used a brass punch to drive the pinion down into the yolk. This seems to have worked, though I guess I'll find out if it did any damage to the pinion soon
. Now that it's been pressed on ones, the bearing is tight fit but can be pulled off by hand with some effort.
Will definitely be sanding down the next outer on my D30 today.
The final pattern still looked good, though if I had some smaller shims, I'd like to remove 0.001 from the inner race, but I'm going to get the D30 installed to get a bit more experience (front's way less important) and perhaps come back to the rear once I'm less psychotic about the whole situation yesterday