Lincoln
July 7th, 2006, 22:28
'89 OMC 2.3 liter I/O. Carb'd and a points distributor. Overhead cam Ford block. Roughly 200 hours use.
Taken out about 3 weeks ago and ran fine until the end of the day then started running a little weird. Kind of short on power.
Taken out last weekend and ran find for 15 minutes then started running bad. Low on power, rough, etc. Continued to get worse on the way back to the dock until it quit running completely and wouldn't restart.
Cooled overnight and started but ran extremely rough. Some close detective work found oil leaking out of the coil. Thought I was extremely smart and went down and bought another coil.
Being the cool guy I am I bought an MSD coil. The original was an external resistor coil which was the same as the MSD but I could not find a resistor anywhere. There was about a 1/4 volt drop from the battery to the positive lead on the coil. Wrote that off as a voltage drop in the wiring and added the MSD .8 ohm resistor before the coil.
Boat still runs crappy and smells rich. It will barely come off an idle and likes to drop off sudenly and backfire. No high revs.
I messed around checking the plug wires and also pulling one at a time to see if I could find a miss firing cylinder. On all four none really seemed to change the way it was running and all the wires checked out.
On another moment of briliance I bypassed the resistor and tried that. It runs a little smoother but still won't come up above 1200 to 1500 rpms. Only ran it for a minute and didn't really give it a chance to back fire. I checked the timing with a timing light and it seems ok. It won't really hold any rpms but it seemed to be around 8-10 degrees and then start advancing towards 20 before basically puking out.
I'm wondering if the timing belt took a crap and jumped a notch. What puzzles me is the running find and slowly getting worse. And also running better when the motors cool than when hot. It does have a 1 quart water seperator/fuel filter and that was replaced before the last weekend trip.
The points look to be gapping out ok but I only checked them visually (before adult beverages were consumed) and didn't checked them with a feeler gauge.
I'm retarded so please help. :D
Taken out about 3 weeks ago and ran fine until the end of the day then started running a little weird. Kind of short on power.
Taken out last weekend and ran find for 15 minutes then started running bad. Low on power, rough, etc. Continued to get worse on the way back to the dock until it quit running completely and wouldn't restart.
Cooled overnight and started but ran extremely rough. Some close detective work found oil leaking out of the coil. Thought I was extremely smart and went down and bought another coil.
Being the cool guy I am I bought an MSD coil. The original was an external resistor coil which was the same as the MSD but I could not find a resistor anywhere. There was about a 1/4 volt drop from the battery to the positive lead on the coil. Wrote that off as a voltage drop in the wiring and added the MSD .8 ohm resistor before the coil.
Boat still runs crappy and smells rich. It will barely come off an idle and likes to drop off sudenly and backfire. No high revs.
I messed around checking the plug wires and also pulling one at a time to see if I could find a miss firing cylinder. On all four none really seemed to change the way it was running and all the wires checked out.
On another moment of briliance I bypassed the resistor and tried that. It runs a little smoother but still won't come up above 1200 to 1500 rpms. Only ran it for a minute and didn't really give it a chance to back fire. I checked the timing with a timing light and it seems ok. It won't really hold any rpms but it seemed to be around 8-10 degrees and then start advancing towards 20 before basically puking out.
I'm wondering if the timing belt took a crap and jumped a notch. What puzzles me is the running find and slowly getting worse. And also running better when the motors cool than when hot. It does have a 1 quart water seperator/fuel filter and that was replaced before the last weekend trip.
The points look to be gapping out ok but I only checked them visually (before adult beverages were consumed) and didn't checked them with a feeler gauge.
I'm retarded so please help. :D